Case Study: Diagnosing the Root Cause for High Vibrations on a Vertical Pump

  • Home
  • Case Study: Diagnosing the Root Cause for High Vibrations on a Vertical Pump

Case Study: Diagnosing the Root Cause for High Vibrations on a Vertical Pump

Author: Tom Calko, P.E., Group Head, Field Service Engineering, Staff Engineer II

Determining the cause of a change in machinery condition can be a difficult task, and vibration analysis is a valuable tool to help determine the reason for these changes.  This article presents a case study to determine the cause of high vibration levels and low reliability of a vertical pump.  The source of the problem was identified as a structurally compliant discharge head and motor adapter connection; increasing the stiffness of both of these items was recommended to resolve this problem.  This case study utilized standard vibration analysis, orbit analysis, operating deflection shape (ODS)/modal testing, and rotor dynamic modeling.

Figure 1: Vertical pump installation

Background

The vertical pumps (Figure 1) were placed into liquid natural gas service in October 2021 and operated with high vibration levels following the initial start-up.  The pumps were originally supplied with 25 stages (impellers).  In this configuration, the pump produced higher pressure and flow than required by the operator.  Operational adjustments were made to reduce this excess head and flow to suitable operating ranges for the piping system.  Operating in this configuration resulted in poor reliability with the motors.  

In January 2022, two stages were eliminated, leaving the pumps with 23 stage impellers.  When the de-staged pumps were re-installed, a tuning plate was installed between the motor base and top of the discharge head to decrease the structural natural frequency of the motor and pump head assembly, since there were concerns about the pump running at a structural natural frequency.  Figure 2 shows the location and assembly of the tuning plate.

When the modified pumps were placed into operation, the motor and pump condition improved, and vibration amplitudes were considerably decreased from prior levels.  However, in November 2023, vibration levels increased on one of the pumps, and higher noise levels were observed.  This pump was shut down and inspected for damage.  During inspection, wear and scoring were observed on the pump shaft and throat bushing in the bottom of the seal chamber.  The throat bushing was replaced, and the pump was placed on stand-by service until it could be completely disassembled and inspected.  In order to determine the source of the problem, E2G performed a machine diagnostic evaluation as described below.

Figure 2: Pump cross section and tuning plate

Field Vibration Analysis

Common measurement locations for housing vibration for vertical pumps are on the upper motor bearing and at the lower motor bearing/upper pump discharge head.  Measurements were obtained at these locations, and amplitudes are summarized below in Table 1.  The dominant frequency of vibration was at the pump running speed (3582 rpm or 59.7 Hz).  The radial vibration amplitudes measured at both locations exceeded the guidelines in Hydraulic Institute Standard 9.6.4 [1].

Permanent proximity probes were not installed on this pump, so E2G installed a set of portable proximity probes and measured the shaft vibration levels.  The measured shaft vibration amplitudes were as high as 6.15 mils pk-pk, which is considered unsatisfactory for long-term continuous operation per ISO 7919-3 [2]. The proximity probe data was also used to generate orbit plots for evaluation of shaft motion during steady state operation.  The orbit plot in Figure 3 shows evidence of two inner loops during a single revolution of the shaft.  These loops typically indicate non-synchronous vibration content, such as a rub-bounce condition, and evidence of rubbing between the shaft and throat bushing was observed during the November 2023 inspection.  Therefore, it was concluded that the internal loops were evidence of these rubs.

Figure 3: Orbit plot showing a completed inner loop and a second inner loop that is partially shown prior to the tachometer trigger

Traditional accelerometer-based data was also collected and used to determine the ODS of the pump and piping assembly.  The shape and relative magnitude of the motor and discharge head deflection at operating speed are shown in Figure 4.  There is a significant amount of deflection at the throat bushing area, which aligns with both the high shaft vibration amplitudes and orbit shape as well as the shaft and bushing damage observed during the shutdown inspection.  Modal testing was completed after the pump was shut down, and this data showed that the structural natural frequency nearest to running speed was at 44 Hz and had a similar mode shape to the ODS as shown in Figure 4.  Since the separation margin between this natural frequency and the operating speed of 59.7 Hz was 26%, the high vibration levels were not attributed to resonant amplification.  Annex E of HI Standard 9.6.8 [3] indicates that a separation margin of 10% is usually satisfactory to avoid unacceptable vibration amplification for all modes.

Figure 4: ODS and mode shape of the motor and discharge head at the maximum displaced location; the unreformed shape is shown in grayscale

From the modal test data, the stiffness of the motor-to-discharge head was determined to be 5,100 lbf/in, which is considered to be a relatively flexible joint.  The ODS and mode shape also show that the lack of stiffness of the discharge head contributes to the problem as well.  The excessive structural compliance was identified as the root cause of the high vibration levels and the shaft-throat bushing rub.  To resolve this problem, E2G recommended increasing the stiffness of the discharge head and motor-discharge head connection while ensuring sufficient separation margin to running speed.

To increase confidence in the conclusions, E2G built a simplified rotor dynamic model of the pump and compared the measured coastdown data against the calculated Bode plot of the model.  This data is shown in Figure 5 and provides a good match to the measured structural natural frequencies of 28 Hz (1675 rpm) and 43 Hz (2550 rpm).  This simple rotor dynamic model provides confirming evidence of the conclusions and recommendations.

Figure 5: Comparison of measured and calculated Bode plot from rotor dynamics model

Summary

This article provides a case study of diagnosing the root cause of excessive machine vibrations.  Vibration analysis is a powerful tool to help understand the source of the problem and identify a high-confidence solution to fix it.  Casing and shaft vibration analysis, orbit analysis, ODS/modal testing, and rotor dynamic modeling were used to identify the problems and verify the proposed solution to increase the discharge head stiffness and increase the motor-discharge head connection stiffness.  

If you have any questions for the author, please submit the form below:

References

  • [1] ANSI/HI 9.6.4-2016, American National Standard for Rotordynamic Pumps for Vibration Measurements and Allowable Values, Hydraulic Institute.
  • [2] BS ISO 7919-3:2009+A1:2017, Mechanical Vibration – Evaluation of Machine Vibration by Measurements on Rotating Shafts.
  • [3] ANSI/HI 9.6.8-2014 (R2021) Rotodynamic Pumps – Guideline for Dynamics of Pumping Machinery.

Newsletter Archive

Access all of our previously published Industry Insights Newsletter articles:

Recently Published

Analysis of Piping Surge Events

Authors: Bob Davis, P.E., Consulting Engineer II; Curtis Koether, P.E., Senior Engineer II

Surge events in piping systems can lead to severe displacements, loud noises, and operational challenges. Using a case study, this article highlights the factors behind surge events, including rapid changes in liquid velocity and pressure, and how forces generated during these transient events can impact piping systems. The authors discuss how a few targeted support modifications effectively resolved these issues without resorting to costly system overhauls or potentially problematic specialty equipment.

Read More »

Addressing Piping Vibration in the Oil, Gas, and Petrochemical Industries: The Upcoming API 579 Part 15

Author: Michael F.P. Bifano, Ph.D., P.E., ISO VCAT-IV, Rotating Equipment, Vibration, & Dynamics Team Leader

With the recent API Fall Meeting, it is timely to revisit this November 2023 article on API 579 Part 15, Methodologies of Piping Vibration, featuring insights from one of the new standard’s co-authors, Mike Bifano. This article discusses the three-tiered evaluation system and explains how vibration fits into a mechanical integrity program. Read more and learn about the highly anticipated improvements to our industry standards.

Read More »

Damage Mechanisms Affecting Catalytic Reformer Units

Author: Chris Aguayo, Team Leader of Materials & Corrosion/Senior Engineer II, M&C

This article offers a detailed look at catalytic reformer units, highlighting key components and operations like octane improvement and hydrogen production. The discussion on damage mechanisms, from high-temperature hydrogen attack to chloride stress corrosion cracking, provides valuable insights and lessons learned from industry experience which address common operational challenges and failures.

Read More »

Reformer MOV Cracking FFS Case Study

Authors: Kraig S. Shipley, P.E., Piping & Fired Heaters Principal Engineer II; Anthony J. Feller, Group Head, Senior Engineer II; Seetha Ramudu Kummari, Ph.D., P.E., Consulting Engineer I

This case study explores fatigue cracking in motor-operated valves (MOVs) used to cycle flow in and out of reformer unit reactors. Surface flaws were discovered during a recent turnaround which prompted further investigation. As only a few of the MOVs were opened and inspected, the owner-user was concerned about the extent and severity of cracks in additional valves. In this article, the authors share the details of the case study and how Equity’s recommendations helped the client make informed repair decisions.

Read More »
Generic selectors
Exact matches only
Search in title
Search in content
Post Type Selectors
Pages
Industry Insights Newsletter Articles
Events
Library Items